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Clean Hydrogen Partnership

Fire in the hydrogenation reactor of a alcohols an acids production plant

Event

Event ID
783
Quality
Description
A fire started on the primary hydrogenation reactor of a chemical plant synthesizing alcohols and acids by reactions between olefins and a H2 / CO gas mixtures. The alcohols are synthesised in 3 steps: HP (280b) / BP (<3b) ozonisation, primary hydrogenation (63b), vacuum distillation and final hydrogenation (63b).

A pressure drop was noted on the hydrogenation unit, caused by a leak from a thermally insulated pipe (DN 50, 3.6 mm). The pipe was containing hydrogen at 40 bar and was connected to a separator. The unit was depressurized, but 15 minutes later the hydrogen ignited generating a jet fire directed towards the inside of the unit.
The emergency plan was triggered, with four water jets cooling the unit. The fire was put under control by means of fire extinguishers do that the firefighters did not need to intervene.

Property damage and environmental impact (smoke) were limited.

An investigation of the pipe has revealed a 30 mm long crack perpendicular to the axis of the pipe in the outer part of an elbow, corrosion I nth direction of the flange of connection with the condenser and also internal corrosion at the elbow. The pipeline was corroded / eroded and the stresses due to insufficient support weakened the elbow. Thickness checks were carried out, the pipe was replaced (5.6 mm thick) and a suitable support was put in place.
Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Fire (No additional details provided)
Macro-region
Europe
Country
France
Date
Root causes
Root CAUSE analysis
INITIATING CAUSE was the self-ignition of hydrogen released via a crack in a pipe.
The crack was probably caused by corrosion and consequent reduction of the stress-bearing section of the pipe.

Facility

Application
Chemical Industry
Sub-application
alcohols and acids production
Hydrogen supply chain stage
All components affected
hydrogen pipe, hydrogenation reactor
Location type
Unknown
Location description
Industrial Area
Operational condition

Emergency & Consequences

Number of injured persons
0
Number of fatalities
0
Post-event summary
Property damage and environmental impact (smoke) were limited.

Lesson Learnt

Corrective Measures

Since the cause was failure to bear stress at a corroded pipe elbow, a thicker tube was used to replace the cracked pipe (5.6 mm thick instead of 3.6) and a suitable support was put in place to reduce stress at the elbow. .

Event Nature

Release type
gas
Involved substances (% vol)
H2 100%
Design pressure (MPa)
4
Presumed ignition source
Not reported
Ignition delay
15 minutes
Deflagration
N
High pressure explosion
N
High voltage explosion
N
Flame type
Jet flame

References

Reference & weblink

ARIA data base <br />
event no. 21196

JRC assessment