Skip to main content
Clean Hydrogen Partnership

hydrogen fire produced by radiolysis

Event

Event ID
496
Quality
Description
On February 3, 1994, a control room operator at Surry Power Station, Unit 1, observed pressure spikes on the pressurizer level instruments. At the same time, a loud rumbling sound was heard in the containment. The containment vent radiation alarm was received, and as a precaution, the containment was evacuated.

At the time of the event, the pressurizer was drained and vented to both the pressurizer relief tank and the containment atmosphere through a filtered covering over the piping where the safety valves had been removed. The reactor vessel head had just been detensioned. There was fuel in the reactor vessel. A modification to eliminate the pressurizer loop seals was in progress.

The pressure fluctuations inside the pressurizer caused the expulsion of radioactive gases from the pressurizer into the containment causing alarms on both the containment radiation monitor and the ventilation radiation monitor where the ongoing filtered containment purge was directed. Licensee personnel calculated the release rate through the monitored ventilation purge path to be approximately 30 percent of the technical specification limits. One worker received an estimated internal exposure of 70 Sv [7 mrems] and a total dose of 160 Sv [16 mrems].

The licensee investigation showed that the screens for excluding foreign material that were taped over the pressurizer side of the piping where the three safety valves were removed were discoloured and appeared burned. The licensee concluded that a hydrogen gas burn had occurred inside the pressurizer. Welding activities associated with the pressurizer loop seal modification had ignited the hydrogen gas that had come out of solution and accumulated inside the pressurizer and associated piping. There were no personnel inquiries.
Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Fire (No additional details provided)
Macro-region
North America
Country
United States
Date
Root causes
Root CAUSE analysis
The licensee concluded that a hydrogen gas burn had occurred inside the pressurizer. Welding activities associated with the pressurizer loop seal modification had ignited the hydrogen gas that had come out of solution and accumulated inside the pressurizer and associated piping.

Facility

Application
Power Plant
Sub-application
Nuclear power plant
Hydrogen supply chain stage
All components affected
nuclear reactor pressuriser,
Location type
Unknown
Location description
Industrial Area
Operational condition
Pre-event occurrences
At the time of the event, the pressurizer was drained and vented to both the pressurizer relief tank and the containment atmosphere through a filtered covering over the piping where the safety valves had been removed. The reactor vessel head had just been detensioned. There was fuel in the reactor vessel. A modification to eliminate the pressurizer loop seals was in progress.

Emergency & Consequences

Number of injured persons
0
Number of fatalities
0

Lesson Learnt

Lesson Learnt

The licensee imposed additional controls for welding on the primary system. These require that samples be taken and analysed before initiating an arc to determine if explosive gasses are present. The licensee also evaluated pressurizer stresses associated with the rapid hydrogen burn and completed a piping support inspection and internal inspection of the pressurizer.

Event Nature

Release type
gas
Involved substances (% vol)
H2 100%
Presumed ignition source
Welding

References

Reference & weblink

Information Notice No. 94-53: Hydrogen Gas Burn Inside Pressurizer During Welding<br />
<br />
Available at https://www.nrc.gov/reading-rm/doc-collections/gen-comm/info-notices/19…

JRC assessment