Skip to main content
Clean Hydrogen Partnership

Explosion at the generator of a coal-fired power plant

Event

Event ID
395
Quality
Description
The incident happened at a 500-megawatt, hydrogen-cooled generator driven by steam turbines. The generator was shut down for maintenance.
A purging procedure had to be executed before starting repair and maintenance works, consisting of (1) purging the hydrogen cooling loop of the generator with carbon dioxide, (2) measuring the CO2 concentrations by a densitometer to verify the complete removal of hydrogen, and (3) purging the generator with air, after which maintenance could be performed.

The CO2 reading was reported to be 100% CO2 at the top of the generator. The cooling system was then purged with air, after which a 1/2-in. (1.3-cm) pipe in the cooling loop was cut to install some new instrumentation. When the pipe was cut, pressurised gas was emitted. Workers assumed that the gas was either carbon di-oxide or air and proceeded with the new instrument installation. However, there was still at least some hydrogen in the pipe and the rest of the cooling loop. When the welder struck an arc, a flame developed at the pipe opening and flashed back into the generator. This caused a low-level explosion within the generator shroud.

[Zalosh and Short, 1978]
Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Macro-region
North America
Country
United States
Date
Main component involved?
Pipe
How was it involved?
Internal Explosion (H2-Air Mixture)
Initiating cause
Inadequate Or No Purge
Root causes
Root CAUSE analysis
The INITIATING CAUSE was an explosion during maintenance works, due to residual presence of hydrogen despite the purging action performed before.

The ROOT CAUSE was an ineffective purge procedure, and the lack of ‘second opinion’ measure such a direct measure of gas composition.

Facility

Application
Power Plant
Sub-application
coal-fired power plant
Hydrogen supply chain stage
All components affected
generator and its internal components
Location type
Confined
Location description
Unknown
Operational condition

Emergency & Consequences

Number of injured persons
0
Number of fatalities
0
Currency
US$
Property loss (onsite)
150000
Post-event summary
The explosion damaged ventilation baffle plates and auxiliary equipment in the generator so that it was out of service for 26 days.

Lesson Learnt

Lesson Learnt
Zalosh and Short (1978, see References) concluded the presentation of this exemplary case, by remarking the difficulty to guarantee large and complex equipment free of hydrogen. Purging is based on the base of mixing and dilution, but it is improbable that it could occur uniformly and completely in closed spaces containing small diameter gas paths, curves and dead ends. Therefore, additional precautions must be taken, before operation such welding are performed in air. One of the precautions could consist in direct concentration measurements of hydrogen, not (only) CO2, performed at several locations, and in particular t the place where works are planned.

Event Nature

Release type
gas mixture
Involved substances (% vol)
H2,
CO2
Actual pressure (MPa)
low
Design pressure (MPa)
low
Ignition delay
Electricity

References

Reference & weblink

Reported at Section 2.4 of Zalosh and Short report: <br />
COMPARATIVE ANALYSIS OF HYDROGEN FIRE AND EXPLOSION INCIDENTS<br />
Quarterly Report No. 2 for Period December 1, 1977 - February 28, 1978<br />
https://www.osti.gov/biblio/6566131<br />
(accessed September 2020)

Also uptaken in US database H2TOOLS<br />
https://h2tools.org/lessons/improper-purging-procedure-results-hydrogen… />
(accessed Decembr 2025)

JRC assessment