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Clean Hydrogen Partnership

Explosion in coating spray equipment

Event

Event ID
300
Quality
Description
An explosion occurred in the heat treatment workshop of this site. The explosion was centred in the electrical control panel of the High Velocity Oxy Fuel (HVOF) thermal spraying equipment.
The violent explosion propelled shrapnel, killing one person present.
Four further personnel were injured.

The hydrogen, leaked from a loose connection on the flashback arrestor of the unit, then migrated into the upper compartment of the HVOF console. At the point, an explosion when the hydrogen was ignited by a spark from any one of the electrical switches or relays contained there.

The leaking connection was on a component which in all probability had only just been replaced. It is probable that the new arrestor, tightened the connections by hand and intended to tighten them with a spanner later but forgot to do so.
Two recently drilled holes in the barrier partition of the HVOF console provided a potential leakage path for hydrogen into the electrical cabinet.
Purge air which is intended to pressurise the electrical cabinet to prevent flammable gas ingress was not connected at the time of the explosion.
The hydrogen pipework had not been leak tested prior to recommissioning.
Safety systems to prevent flammable gas ingress into the electrical cabinet had been disconnected or bypassed.
Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Macro-region
Europe
Country
United Kingdom
Date
Root causes
Root CAUSE analysis
The INITATING CAUSE was a loose hydrogen connection, probably due to the fact that it had not been tightened when replacing the connection.
The ROOT CAUSES were a combination of lack of safety measures, shortcoming in the existing procedure and modification to the facility without executing a new risk assessment.

Facility

Application
Chemical Industry
Sub-application
Coating production
Hydrogen supply chain stage
All components affected
High Velocity Oxy Fuel (HVOF) spray machine.
Location type
Unknown
Location description
Industrial Area
Operational condition
Pre-event occurrences
Under normal operation, the upper compartment of the HVOF console would have been supplied with purge air and any holes in the central dividing panel would have been sealed by the presence of valves and other components. The purge air was not connected. Under normal circumstances, the lack of purge air pressure and open door would prevent the unit from operating. However, these two safety devices were observed to have been bypassed.

Description of the facility/unit/process/substances
DESCRIPTION OF THE FACILITY
A high velocity oxy-fuel spray machine (HVOF) is a thermal spray processes using a mixture of a gaseous fuel and oxygen. The gas can be hydrogen, methane, propane, propylene, acetylene, natural gas, etc.
The mixture is fed into a combustion chamber, where it is ignited and combusted continuously. The resultant hot gas at a pressure close to 1 MPa emanates through a converging–diverging nozzle and travels through a straight section.

Emergency & Consequences

Number of injured persons
4
Number of fatalities
1
Investigation comments
According to the investigation, the hydrogen, having leaked from the loose connections on the flashback arrestor of the unit, migrated into the upper compartment of the HVOF console.
An explosion then occurred when it was ignited by a spark from any one of the electrical switches or relays contained there.
The leaking connection was on a component which in all probability had only just been replaced. It is probable that the new arrestor, tightened the connections by hand and intended to tighten them with a spanner later but forgot to do so.
Two recently drilled holes in the barrier partition of the HVOF console provided a potential leakage path for hydrogen into the electrical cabinet.
Purge air which is intended to pressurise the electrical cabinet to prevent flammable gas ingress was not connected at the time of the explosion.
The hydrogen pipework had not been leak tested prior to recommissioning.
Safety systems to prevent flammable gas ingress into the electrical cabinet had been disconnected or bypassed.
Emergency action
The trespassing of the limit of 4% of hydrogen in air triggered the stop of the operations. The diagnostic sstems ansd rhe operative safeguards worked as planned.

Lesson Learnt

Lesson Learnt

Conclusions of the investigation:
1. The hydrogen pipework had not been leak tested prior to recommissioning.
2. Safety systems to prevent flammable gas ingress into the electrical cabinet had been disconnected or bypassed.

Event Nature

Release type
gas
Involved substances (% vol)
H2 100%
Presumed ignition source
Open flame
Deflagration
N
High pressure explosion
N
High voltage explosion
N

References

Reference & weblink

Event description provided by HSE, original source confidential

JRC assessment