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Clean Hydrogen Partnership

Pipe explosion at a hydrogen production unit in a refinery

Event

Event ID
1226
Quality
Description
A fire broke out at a pipe of the hydrogen production unit, belonging to the steam methane reformer part of the fluidised catalytic cracking (FCC) plant. The fire occurred when personnel of a contracting company were executing preparing maintenance works. For this, they had to open a hydrogen-carrying pipe at a flange and blind both opening with bolted steel plate. The pipe was still containing residual hydrogen, which ignited when the pipe was opened.

Valves connected to the affected pipe were shut off. Fire authorities mobilized 25 personnel and 23 pieces of equipment to extinguish the blaze, which was fully contained approximately 20 minutes later. After suppression, further efforts were continued by spraying water on the pipeline to avoid secondary accidents.
Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Fire (No additional details provided)
Macro-region
Asia
Date
Main component involved?
Flange
Initiating cause
Inadequate Or No Purge
Root causes
Unknown (No additional details provided)
Root CAUSE analysis
The INITATING CAUSE was the opening of a hydrogen pipe containing still residual hydrogen.

The results of the legal investigation are not (yet) known and still several questions are open. Why was there was still hydrogen in the pipe? Was this the result of a wrong purge, or was the wrong pipe to be maintained? Were the actions under the exclusive responsibility of the subcontractor, or was the plant management responsible for unclear instruction and process?

Facility

Application
Petrochemical Industry
Sub-application
SMR
Hydrogen supply chain stage
All components affected
pipe, flange
Location type
Semiconfined
Location description
Industrial Area
Operational condition

Emergency & Consequences

Number of injured persons
3
Number of fatalities
2
Environmental damage
0
Property loss (offsite)
0

Event Nature

Release type
gas
Involved substances (% vol)
H2 100%
Presumed ignition source
Not reported

References

Reference & weblink

The Chosun daily<br />
https://www.chosun.com/english/national-en/2025/10/17/N3WXHD2QYVEZBNPIA… <br />
(accessed October 2025)

Fuel Cells Works news <br />
https://fuelcellsworks.com/2025/10/17/h2/explosion-at-sk-energy-s-ulsan… />
(accesed October 2025)

Hydrogen Insight news of 20 & 24 October 2025<br />
https://www.hydrogeninsight.com/industrial/more-details-emerge-about-ca… />
(accessed October 2025)

JRC assessment