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Clean Hydrogen Partnership

Leak at the generator of a nuclear power plant

Event

Event ID
792
Quality
Description
A leak started on the hydrogen coolant circuit of one of the power generators of the plant. It was indirectly detected thanks to the increased need to generate new hydrogen for cooling. The trend kept growing in the following days. After attempts to isolate the leak, the operator decided to shut down the turbine-generator unit and replaced all the hydrogen coolers.

This is a more detailed sequence of events:
28 August – First signal of an increased make-up rate of hydrogen cooling gas to the main generator. The normal make-up rate of hydrogen was approximately 600 standard cubic feet per day (SCFD). This increase was an indication of hydrogen losses due to a leak.
Technicians sampled areas of the turbine building confirming absence of an explosive mixture. They verified through periodic tours of the turbine building that no welding, cutting, or grinding was being conducted that could result in an ignition source for any potential hydrogen concentration build-up in the turbine building.
10 September - Make-up rate of hydrogen increased to approximately 4,000 SCFD by September 10, 2002. The operator tried unsuccessfully to isolate the hydrogen cooler suspected to leak.
11 September – After unsuccessful attempts to isolate the hydrogen leak, the operator decided to take the unit off-line to implement a repair., The power was reduced to approximately 10% and the generator was taken off-line.
13 September - All four generator hydrogen coolers were replaced, and the unit was restored to full power operations.
Event Initiating system
Classification of the physical effects
Unignited Hydrogen Release
Nature of the consequences
Leak No Ignition (No additional details provided)
Macro-region
North America
Country
United States
Date
How was it involved?
Leak & Formation Of A Flammable H2-Air Mixture
Initiating cause
Unknown
Root causes
Unknown (No additional details provided)

Facility

Application
Power Plant
Sub-application
Nuclear power plant - PWR
Hydrogen supply chain stage
All components affected
hydrogen cooler
Location type
Confined
Location description
Industrial Area
Operational condition
Description of the facility/unit/process/substances
The nuclear power plant consisted in two four-loop Westinghouse pressurized water reactors .
• Units 2 was completed in 1974 with capacity of 1,032 MWe.
• Units 3 was completed in 1976, with a of 1,051 MWe.

DESCRIPTION OF THE GENERATOR COOLING SYSTEM
In a typical H2 coolant system, the hydrogen circulates in a loop between the generators and the coolers, which function are heat exchangers which bring the temperature of the hot hydrogen exiting the generator loop back to near room temperature.
Due to unavoidable hydrogen minor losses, the hydrogen in the circuit has to be topped up by make-up hydrogen, which can be produced onsite and/or supplied by an onsite storage system o be regularly replaced via delivery. The NRC report does not specify which make-up system was present in this plant. The daily need for make-up hydrogen was approximately 1.5 kg. During the reported event, the daily losses were amounting at almost one order of magnitude more (10 kg/d). A New York Times news was reporting a value of 25 kg/d.

The fact that all four were replaced induce to conclude that the loss of hydrogen was occurring there.

Emergency & Consequences

Number of injured persons
0
Number of fatalities
0
Environmental damage
0
Property loss (onsite)
low
Property loss (offsite)
0
Post-event summary
The damage was limited to the loss of electricity production suring few days, and the reapclements of 4 hydrogen coolers.

Event Nature

Release type
gas
Involved substances (% vol)
H2 100%
Release rate
10 kg/d
Released amount
50 kg
Design pressure (MPa)
4
Presumed ignition source
No ignition

References

Reference & weblink

NRC report on inspection of 28 September 2008<br />
https://www.nrc.gov/docs/ML0231/ML023100502.pdf <br />
(accessed Devember 2025)

JRC assessment