Event
- Event ID
- 972
- Quality
- Description
- The event occurred in a bus garage when carrying out the purging process of the hydrogen cylinders. This process was executed via an electronic control system, but it was found that one cylinder solenoid valve was mechanically stuck. In these cases, the valve manufacturer has foreseen an alternative manual process using an override tool. The process was executed according to manufacturer’s instruction, but the valve did not start to evacuate hydrogen when expected.
The fuel cell engineer tried to rectify the problem and started removing the override tool, but forgot to unwind the stem. The sealing O-ring of the tool was damaged and caused a hydrogen release in the vicinity of the manual override tool.
The building was evacuated, the extraction fans set manually and the main shutters open to assist with ventilation and dilution of the hydrogen leak.
During the incident the emergency services were alerted. The fire brigade could monitor hydrogen concentration. The highest hydrogen level recorded was 46% of the lower flammable limit on one sensor located directly above the leak.
therefore levels were judged acceptable from an explosive risk perspective.
Approximately 5 hours later the fire brigade left the site and the depot retuned to normal business, but still subject to the control actions until depletion of the remaining hydrogen. - Event Initiating system
- Classification of the physical effects
- Unignited Hydrogen Release
- Nature of the consequences
- Leak No Ignition (No additional details provided)
- Macro-region
- Europe
- Country
- United Kingdom
- Date
- Root causes
- Root CAUSE analysis
- The initiating cause, as established by the investigation of the valve manufacturing, was the broken wire of the solenoid coil.
Contributing cause was the failing of the manual override tool process to release the hydrogen from the tank. What it followed was an error by the engineer in an attempt to dismantle the manual tool. This caused the damage of an O-ring.
Facility
- Application
- Road Vehicles
- Sub-application
- Hydrogen bus
- Hydrogen supply chain stage
- All components affected
- on-board compressed hydrogen storage
- Location type
- Confined
- Operational condition
- Pre-event occurrences
- The bus was in the garage (depot) for defueling.
The manual purging process had been previously undertaken unsuccessfully a few times by the fuel cell engineers. This was a rare, but not exceptional process.
Emergency & Consequences
- Number of injured persons
- 0
- Number of fatalities
- 0
- Post-event summary
- There has not been any consequence.
- Investigation comments
- The bus company requested by the valve manufacturer to investigate the solenoid valve and to issue a report.
Lesson Learnt
- Lesson Learnt
According to the valve manufacturer,
(1) the solenoid valves of the type mounted on the buses were not fabricated anymore, but were still supported and did not represent any additional hazard than their new version.
(2) The manual tool was safe provided the instructions were thoroughly followed.
To ensure that this will happen in the future, a new detailed procedure was issued in case of failure of the solenoid valve. One new procedure step is the execution of the manual operation outside the depot, to ensure maximal hydrogen dispersion.
This incident is basically a near miss with non negligible hydrogen release) highlights the difficult to build a trustful supply chain for all components and sub-components i an period in which the components and systems have not yet achieved the mass production rates making easy quantification of failure statistics and identification of all possible failure modes.
Event Nature
- Release type
- gas
- Involved substances (% vol)
- H2 100%
- Presumed ignition source
- No ignition
References
- Reference & weblink
Report provided but confidential
JRC assessment
- Sources categories
- Investigation report