Event
- Event ID
- 783
- Quality
- Description
- A fire started on the primary hydrogenation reactor of a chemical plant synthesizing alcohols and acids by reactions between olefins and a H2 / CO gas mixtures. The alcohols are synthesised in 3 steps: HP (280b) / BP (<3b) ozonisation, primary hydrogenation (63b), vacuum distillation and final hydrogenation (63b).
A pressure drop was noted on the hydrogenation unit, caused by a leak from a thermally insulated pipe (DN 50, 3.6 mm). The pipe was containing hydrogen at 40 bar and was connected to a separator. The unit was depressurized, but 15 minutes later the hydrogen ignited generating a jet fire directed towards the inside of the unit.
The emergency plan was triggered, with four water jets cooling the unit. The fire was put under control by means of fire extinguishers do that the firefighters did not need to intervene.
Property damage and environmental impact (smoke) were limited.
An investigation of the pipe has revealed a 30 mm long crack perpendicular to the axis of the pipe in the outer part of an elbow, corrosion I nth direction of the flange of connection with the condenser and also internal corrosion at the elbow. The pipeline was corroded / eroded and the stresses due to insufficient support weakened the elbow. Thickness checks were carried out, the pipe was replaced (5.6 mm thick) and a suitable support was put in place. - Event Initiating system
- Classification of the physical effects
- Hydrogen Release and Ignition
- Nature of the consequences
- Fire (No additional details provided)
- Macro-region
- Europe
- Country
- France
- Date
- Root causes
- Root CAUSE analysis
- INITIATING CAUSE was the self-ignition of hydrogen released via a crack in a pipe.
The crack was probably caused by corrosion and consequent reduction of the stress-bearing section of the pipe.
Facility
- Application
- Chemical Industry
- Sub-application
- alcohols and acids production
- Hydrogen supply chain stage
- All components affected
- hydrogen pipe, hydrogenation reactor
- Location type
- Unknown
- Location description
- Industrial Area
- Operational condition
Emergency & Consequences
- Number of injured persons
- 0
- Number of fatalities
- 0
- Post-event summary
- Property damage and environmental impact (smoke) were limited.
Lesson Learnt
- Corrective Measures
Since the cause was failure to bear stress at a corroded pipe elbow, a thicker tube was used to replace the cracked pipe (5.6 mm thick instead of 3.6) and a suitable support was put in place to reduce stress at the elbow. .
Event Nature
- Release type
- gas
- Involved substances (% vol)
- H2 100%
- Design pressure (MPa)
- 4
- Presumed ignition source
- Not reported
- Ignition delay
- 15 minutes
- Deflagration
- N
- High pressure explosion
- N
- High voltage explosion
- N
- Flame type
- Jet flame
References
- Reference & weblink
ARIA data base <br />
event no. 21196
JRC assessment
- Sources categories
- ARIA