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Clean Hydrogen Partnership

Fire on a heat exchanger at refinery

Event

Event ID
835
Quality
Description
In a petrochemical plant, visual inspection detects fumes under the heat insulation of a heat exchanger operating under hydrogen pressure.
The first intervention team was mobilized and the unit stopped for depressurization and cooling.
A risk analysis was conducted before erecting a scaffold, decalcifying the exchanger and inspecting it under safe conditions. After having defined the fire protection and fire prevention strategy, the operator decided to put the unit back under pressure.
During this rise in pressure, a resumption of fire on the flange justified the triggering of the emergency plan. The intervention team managed the fire.
No injuries or impacts outside the site are to be deplored.
At the time of the accident, the plant was shut down due to a staff strike. The unit, usually operated under a mixture of butane and hydrogen, according to the supplier's recommendations, was filled with hydrogen only.

Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Fire (No additional details provided)
Macro-region
Europe
Country
France
Date
Root causes
Root CAUSE analysis
A leaking seal on a flange is the cause of the accident.

Facility

Application
Petrochemical Industry
Sub-application
hydrogen heat exchanger
Hydrogen supply chain stage
All components affected
heat exchanger operating under hydrogen pressure
Location type
Open
Location description
Industrial Area
Operational condition
Pre-event occurrences
At the time of the accident, the plant was shut down due to a staff strike. The unit, usually operated under a mixture of butane and hydrogen, was filled with pure hydrogen according to supplier's recommendations.

Emergency & Consequences

Number of injured persons
0
Number of fatalities
0
Post-event summary
No injuries or impacts outside the site are to be deplored. At the time of the accident, the plant was shut down due to a staff strike.

Lesson Learnt

Corrective Measures

The action plan put in place to reduce the probability of re-occurrence of the accident comprises:
1. the study of the possibility of cooling and re-pressurizing the heat exchanger under helium or nitrogen,
2. preventive replacement of all connections under hydrogen
3. regular technical inspection.

Event Nature

Release type
gas
Involved substances (% vol)
H2 100%
Presumed ignition source
Not reported

References

Reference & weblink

ARIA data base <br />
event no. 26429

JRC assessment