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Clean Hydrogen Partnership

Fire in a in a fertiliser manufacturing plant

Event

Event ID
983
Quality
Description

The incident took place on the reforming furnace unit of the plant. Around 23:30 pm, during a normal inspection tour, an operator detected a fire on a section of a steam line.
The operator immediately informed the control room. The unit was reduced in speed, with process parameters monitored to ensure that the situation did not worsen. Steam hoses were used in the direction of the flame and the identified hot spots. The next morning at around 6:00 am, the unit was progressively shut down and the fire extinguished.

The fire occurred in one of the boxes containing the header of on one of the reforming tubes bundle. Th efire did not have impact on the surrounding area or equipment.
Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Fire (No additional details provided)
Macro-region
Europe
Country
France
Date
Main component involved?
Flange (Bolts)
How was it involved?
Leak & Formation Of A Flammable Syngas-Air Mixture
Initiating cause
Loss Of Tightness (Thermal Stress/Cycling)
Root causes
Unknown (No additional details provided)
Root CAUSE analysis

An investigation of the causes, carried out after the removal of the affected vessel, showed a leak on a weakened flange. The gasket was intact, no trace of leakage was detected.
Therefore The INITIATING CAUSE was a leaking flange which had partially loosened, possibly due to differential thermal dilatation.

Facility

Application
Chemical Industry
Sub-application
Steam methane reforming
Hydrogen supply chain stage
All components affected
reformer unit, gasket
Location type
Unknown
Location description
Industrial Area
Operational condition
Description of the facility/unit/process/substances
DESCRIPTION IOF THE REFORMING UNIT
The reforming furnace unit consisted of 198 tubes containing a catalyst. Each furnace contained 11 headers on which 18 reforming tubes were welded. Each header was enclosed in a box and fed the transfer line to the secondary reforming.

Emergency & Consequences

Number of injured persons
0
Number of fatalities
0

Event Nature

Release type
gas mixture (syngas)
Involved substances (% vol)
H2,
CH4,
CO,
CO2
Presumed ignition source
Not reported

References

Reference & weblink

Event description no 53561 in the French database ARIA (accessed October 2021)

JRC assessment