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Clean Hydrogen Partnership

Explosion on an ammonia reactor of a fertilizers plant.

Event

Event ID
786
Quality
Description
An explosion, accompanied by abundant black smoke, occurred at an ammonia production plant. An ignited leak of hydrogen in the ammonia production unit had spread to the pressure circuit carrying synthesis gas(mixture of nitrogen N2, H2 and NH3 already synthesized), damaging the hydrogen compressor .
7 operators on site at that moment operated the emergency stop and evacuated the unit to the fall-back zone (reinforced control room), due the risk of a toxic leak.
The plant operator triggered the emergency plan around 20 minutes later, alerted the public rescue service and the crisis team of the prefecture. Firefighters took over from the in-house firefighters who were watering the accident unit with three water spears to prevent the spread of the fire.
In the control room, the production team flushed the synthesis gas circuit with nitrogen to remove the hydrogen and stopped the machines in the workshop while a lower secondary explosion occurred. The operator closed the water networks of the site to avoid pollution of the river Seine by the extinction water. For lack of fuel, the fire went down gradually around one hour after its start.

Toxicity measurements (NH3) were performed in the unit and around the site by fixed and mobile sensors. While downwind around the site the measurements did not reveal any dangerous concentration; 200 ppm was measured in the machine room of the accident unit (the toxicity threshold is at of 345 ppm for a 1 hour exposure). Characteristic NH3 odours were perceptible off site. the NH3 concentrations were zero at the level of the accident unit which was put in cold stop. Half hour later toxicity was back to zero.
Event Initiating system
Classification of the physical effects
Hydrogen Release and Ignition
Nature of the consequences
Macro-region
Europe
Country
France
Date
Main component involved?
Pipe
How was it involved?
Rupture
Root causes
Unknown (No additional details provided)
Root CAUSE analysis
The INITIATING CAUSE could have been one of two options:
(1) A rupture of a pipe near a valve carrying synthesis gas at 200 bar near a compressor of the unit, causing a high pressure burst perceived as an explosion, or
(2) A gas release following by an unconfined vapour cloud explosion.
After loss of confinement, the ignited hydrogen spread around the pipe affected pipe.

The ROOT CAUSE is unknown.

Facility

Application
Chemical Industry
Sub-application
Ammonia production
Hydrogen supply chain stage
All components affected
pipe, compressor
Location type
Unknown
Location description
Industrial Area
Operational condition
Pre-event occurrences
An accident due to pneumatic bursting on a pressure steam pipe had occurred on the same unit in June 2010 (ARIA 38831).
Description of the facility/unit/process/substances
DESCIPTION OF THE SITE
The plant was specialised in the manufacture of fertilisers from four raw materials: natural gas, ammonia, sulfuric acid, and phosphoric acid.
The four main manufacturing units were:
− an ammonia manufacturing unit with a capacity of 1,200 t/day;
− two nitric acid manufacturing units with a capacity of 3,000 t/day;
− an ammonium nitrate manufacturing unit with a capacity of 2,100 t/day;
− a specialty fertilizer (NS/NP) manufacturing unit with a capacity of 2,000 t/day.

The hydrogen required for the production of ammonia was produced from the natural gas by Steam Methane Reforming.

Emergency & Consequences

Number of injured persons
4
Number of fatalities
0
Currency
Euro
Property loss (onsite)
> 5000000
Post-event summary
The 4 injuries were minor. Following an emotional shock, 4 employees who worked on or near the area shortly before the explosion felt bad at the end of the intervention and were examined in the infirmary of the site.

The blast of the explosion damaged a cinderblock wall close to the compressor. The sheet metal roof of the room was reached by the thermal effects of the fire. The compressor was also damaged as a result of its abrupt shutdown and overheating of its oil-free axles. The supply of NH3 was vital for the synthesis of different nitrogen fertilizers, the site loses for several weeks 40% of its production capacity (several million Euros loss). As this plant supplied a large part of the French nitrate nitrogen fertilizer market, the price of these fertilizers increased significantly during this period.

There was no noticeable damage to the environment.


Official legal action
A press release from the prefecture announcing the smells, the absence of toxic effects and the control of the accident was sent at 10:40, while an automatic telephone message informed the mayors of local communities. The emergency plan was raised at 10:55. The operator held a press conference with the prefecture for the benefit of the numerous local and national media who visited the site; information and photos of the accident taken by local residents were circulating on the Internet since 10 am. The management of the site apologized to the residents for the inconvenience caused by the accident. Firefighters left around 11:50.

Lesson Learnt

Lesson Learnt
This specific accident did not generate lessons, at least they are not provided in the ARIA report, and in absence of detail repeated to the technical reason for the leak or rupture of the pipe, HIAD cannot perform its own analysis.

In 2010, one before this incident, another type of incident had brought to a long stop of the ammonia production unit, followed by a detailed analysis of the causes. It was not a hydrogen-related one; a high-pressure failure of a stem container was at that time the initiating cause. The investigation had found shortcomings in material safety document control and traceability. The company could not find the original pipe construction files. The documentation was starting after 25 years since the first commissioning.

Upon request of the authority, the operator performed an inventory of pipes likely to contain non-compliant steels, or at risks of hydrogen (syngas) cracking corrosion. An analysis identifies 65 critical pieces of equipment, which brought to almost 700 material analysed using a portable X-ray analyser (sections of pipes, welds and equipment such as bosses, tees, elbows, etc.). Critical location such bended and curves were also assessed by magnetic particle inspection methods.

This work suggests (but cannot completely exclude) that the failure of a high-pressure pipe on the hydrogen recycle line one year after this thorough analysis and assessment work was not related with material defect or ageing, but possibly to failure in some connection.

A more general lesson learnt is related to the sharing of description of a safety-related event in the public domain. Almost always an event is captured and filed by a repository or a database soon after its occurrence, when the inspection has not even started, or not yet provided conclusions on root causes and recommendations for corrective actions. The investigation works could take several years, and is very seldom re-emerging I the public domain, especially if a legal process is involved. This lowers dramatically the chance to achieve a useful return of experience able to inform the technical community.

Event Nature

Release type
gas mixture (syngas)
Involved substances (% vol)
H2,
N2,
NH3
Release duration
unknown
Actual pressure (MPa)
20
Design pressure (MPa)
20
Presumed ignition source
Not reported

References

Reference & weblink

event no. 41025 of ARIA database:<br />
https://www.aria.developpement-durable.gouv.fr/accident/41025/<br />
(accessed Oct 2025)

For a description of the facility and the safety assessment performed by the plant operator in 2010, after the occurrence of a previous incident, see the full report of ARIA 38959<br />
https://www.aria.developpement-durable.gouv.fr/wp-content/files_mf/FD_3… <br />
(accessed Oct 2025)

JRC assessment